Klähn, Lukas and Meyer, Robert and Tapken, Ulf (2024) Inflow distortion noise and turbulence measurements in a low speed fan test rig. In: 30th AIAA/CEAS Aeroacoustics Conference, 2024. American Institute of Aeronautics and Astronautics. 30th AIAA/CEAS Aeroacoustics Conference, 2024, 2024-06-04 - 2024-06-07, Rom, Italien. doi: 10.2514/6.2024-3157. ISBN 978-162410720-7.
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Official URL: https://arc.aiaa.org/doi/10.2514/6.2024-3157
Abstract
In the context of emerging aircraft with boundary layer ingestion and high bypass ratios, fan broadband noise is expected to increase. On the one hand, broadband noise is excited when the ingested turbulence interacts with the rotor. On the other hand the distorted mean flow in the inlet affects the turbulence generated by the rotor, i.e. the rotor wakes and the tip vortex. In this study turbulence measurements upstream and downstream of the rotor with hot wires are combined with an in-duct sound power measurement technique in a laboratory fan test bench. The sound power is calculated based on a broadband radial mode analysis. Based on the increased turbulence measured downstream of the rotor, the rotor stator interaction is expected to increase with inflow distortion. The sound power measurements do not confirm this expectation. The reason for this contradiction are discussed in the paper. It is assumed that the rotor stator interaction noise is masked by the turbulence rotor interaction noise at high frequencies and possibly by low frequency stall noise that arises when the rotor blade passes through the inflow distortion. These assessments are supported by the hot wire measurements.
| Item URL in elib: | https://elib.dlr.de/210620/ | ||||||||||||||||
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| Document Type: | Conference or Workshop Item (Speech) | ||||||||||||||||
| Title: | Inflow distortion noise and turbulence measurements in a low speed fan test rig | ||||||||||||||||
| Authors: |
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| Date: | June 2024 | ||||||||||||||||
| Journal or Publication Title: | 30th AIAA/CEAS Aeroacoustics Conference, 2024 | ||||||||||||||||
| Refereed publication: | Yes | ||||||||||||||||
| Open Access: | Yes | ||||||||||||||||
| Gold Open Access: | No | ||||||||||||||||
| In SCOPUS: | Yes | ||||||||||||||||
| In ISI Web of Science: | No | ||||||||||||||||
| DOI: | 10.2514/6.2024-3157 | ||||||||||||||||
| Publisher: | American Institute of Aeronautics and Astronautics | ||||||||||||||||
| ISBN: | 978-162410720-7 | ||||||||||||||||
| Status: | Published | ||||||||||||||||
| Keywords: | Inflow distortion; turbulence; BLI; CRAFT; fan noise; hot wire measurement; acoustic mode detection | ||||||||||||||||
| Event Title: | 30th AIAA/CEAS Aeroacoustics Conference, 2024 | ||||||||||||||||
| Event Location: | Rom, Italien | ||||||||||||||||
| Event Type: | international Conference | ||||||||||||||||
| Event Start Date: | 4 June 2024 | ||||||||||||||||
| Event End Date: | 7 June 2024 | ||||||||||||||||
| HGF - Research field: | Aeronautics, Space and Transport | ||||||||||||||||
| HGF - Program: | Aeronautics | ||||||||||||||||
| HGF - Program Themes: | Clean Propulsion | ||||||||||||||||
| DLR - Research area: | Aeronautics | ||||||||||||||||
| DLR - Program: | L CP - Clean Propulsion | ||||||||||||||||
| DLR - Research theme (Project): | L - Future Engines and Engine Integration, L - Components and Emissions | ||||||||||||||||
| Location: | Berlin-Charlottenburg | ||||||||||||||||
| Institutes and Institutions: | Institute of Propulsion Technology > Engine Acoustic | ||||||||||||||||
| Deposited By: | Klähn, Lukas | ||||||||||||||||
| Deposited On: | 09 Jan 2025 11:37 | ||||||||||||||||
| Last Modified: | 09 Jan 2025 11:37 |
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