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Inflow distortion noise and turbulence measurements in a low speed fan test rig

Klähn, Lukas and Meyer, Robert and Tapken, Ulf (2024) Inflow distortion noise and turbulence measurements in a low speed fan test rig. In: 30th AIAA/CEAS Aeroacoustics Conference, 2024. American Institute of Aeronautics and Astronautics. 30th AIAA/CEAS Aeroacoustics Conference, 2024, 2024-06-04 - 2024-06-07, Rom, Italien. doi: 10.2514/6.2024-3157. ISBN 978-162410720-7.

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Official URL: https://arc.aiaa.org/doi/10.2514/6.2024-3157

Abstract

In the context of emerging aircraft with boundary layer ingestion and high bypass ratios, fan broadband noise is expected to increase. On the one hand, broadband noise is excited when the ingested turbulence interacts with the rotor. On the other hand the distorted mean flow in the inlet affects the turbulence generated by the rotor, i.e. the rotor wakes and the tip vortex. In this study turbulence measurements upstream and downstream of the rotor with hot wires are combined with an in-duct sound power measurement technique in a laboratory fan test bench. The sound power is calculated based on a broadband radial mode analysis. Based on the increased turbulence measured downstream of the rotor, the rotor stator interaction is expected to increase with inflow distortion. The sound power measurements do not confirm this expectation. The reason for this contradiction are discussed in the paper. It is assumed that the rotor stator interaction noise is masked by the turbulence rotor interaction noise at high frequencies and possibly by low frequency stall noise that arises when the rotor blade passes through the inflow distortion. These assessments are supported by the hot wire measurements.

Item URL in elib:https://elib.dlr.de/210620/
Document Type:Conference or Workshop Item (Speech)
Title:Inflow distortion noise and turbulence measurements in a low speed fan test rig
Authors:
AuthorsInstitution or Email of AuthorsAuthor's ORCID iDORCID Put Code
Klähn, LukasUNSPECIFIEDhttps://orcid.org/0000-0002-1425-4453175332753
Meyer, RobertUNSPECIFIEDhttps://orcid.org/0009-0005-5241-1818175332755
Tapken, UlfUNSPECIFIEDhttps://orcid.org/0000-0002-0870-1253175332757
Date:June 2024
Journal or Publication Title:30th AIAA/CEAS Aeroacoustics Conference, 2024
Refereed publication:Yes
Open Access:Yes
Gold Open Access:No
In SCOPUS:Yes
In ISI Web of Science:No
DOI:10.2514/6.2024-3157
Publisher:American Institute of Aeronautics and Astronautics
ISBN:978-162410720-7
Status:Published
Keywords:Inflow distortion; turbulence; BLI; CRAFT; fan noise; hot wire measurement; acoustic mode detection
Event Title:30th AIAA/CEAS Aeroacoustics Conference, 2024
Event Location:Rom, Italien
Event Type:international Conference
Event Start Date:4 June 2024
Event End Date:7 June 2024
HGF - Research field:Aeronautics, Space and Transport
HGF - Program:Aeronautics
HGF - Program Themes:Clean Propulsion
DLR - Research area:Aeronautics
DLR - Program:L CP - Clean Propulsion
DLR - Research theme (Project):L - Future Engines and Engine Integration, L - Components and Emissions
Location: Berlin-Charlottenburg
Institutes and Institutions:Institute of Propulsion Technology > Engine Acoustic
Deposited By: Klähn, Lukas
Deposited On:09 Jan 2025 11:37
Last Modified:09 Jan 2025 11:37

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